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Can't really see it huh?
I had to remove and relocate a few things for the intercooler install. Unfortunately 1 of those things was a washer that forced this stud to protrude a bit more than it was supposed to and pierce a small hole in the condenser. So the 134 leaked out causing the Low Pressure Cycling Switch to stop the operation of the compressor's clutch. Here is a closer look:
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Fully built HRC Turboed 2.4: Wiseco pistons, T2 rods, Port & Polished head (Bob Special) with oversize Stainless Steel valves, #14 Crane Cams, AF/X UDP, 3" custom downpipe, 3" hi flow exhaust No balance shafts, Ported GT intake manifold, Bored Throttle Body, 30lb injectors, Water Injected
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Is that a factory part or a personal mod?
Is it something that other PT owners should inspect on their own cars? (Just asking what others will wonder about if this post shows up in a forum search)
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2002 Dream Cruiser #435 with: over 115hp nitrous, MX-5 "burp-free" shift mod, 2003 shifter, 2001 radio, 2001 Mopar subwoofer, MX-5 designed true cold-air intake, MX-5 designed double platinum spark plugs, shory antenna, much more.... |
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Quote:
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Fully built HRC Turboed 2.4: Wiseco pistons, T2 rods, Port & Polished head (Bob Special) with oversize Stainless Steel valves, #14 Crane Cams, AF/X UDP, 3" custom downpipe, 3" hi flow exhaust No balance shafts, Ported GT intake manifold, Bored Throttle Body, 30lb injectors, Water Injected
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